I have a slight issue with my Quad.
Everthing works fine only my Yaw is still not rock solid after stick input..
When i lift the Quad the heading hold is perfect! no drift at all..
When i rotate with stick input and release the stick it takes a second or so to hold.. it is not a solid hard stop.
I tried to increase P to max of 20 and still this happens..
Can someone steer me in a direction to find this problem?
Im using A Crius Multiwii board with
ITG3205 TRIPLE AXIS GYRO
BMA180 ACCELEROMETER
BMP085 BAROMETER
HMC5883L MAGNETOMETER
Emax 2822 1200kv with 8x4.5 props
Turnigy plush 12A
