Hello all. I am new to the hobby of multirotors and have built a quad using an Emaxx Nighthawk Pro 250 base. I am using a Naze32 rev6, OSDoge and a FRSky D4R-ii receiver. Here is a short video of the issue I am experiencing. https://youtu.be/eco5RTjoASw
Shortly after takeoff I experience a throttle "jitter" and thereafter drop to the ground. The FC is flashing a green LED and I have to disarm then rearm my transmitter and can take off again. This is also using a fully charged 3s Lipo. Any ideas?