hi guys
i just face a problem
i made a quadcopter based on arduino uno and imu 9250
when i compile and run a test on multiwii everythings work fine for the imu
but when i try to react the motor its only beeping 3 times
and when i set up the tortulle there is nothing happend with the motor
but when i attach the esc to the receiver everythings work fine , the motor spin in direct signal to the receiver
im using arduino UNO as the flight control
IMU 9250 as the sensor
Flysky ct6b as the transmitter and receiver
i really need help
i only have 5 days left to final project in my degree
if it wont fly i'll be drop out and fail my university
anyone