Hi everyone,
I try to understand my problem.
I set up a quadricopter:
Motor EMAX CF2822 1200KV Outrunner
FLYING 30A BEC ESC
Gyro ITG3200
ACC BMA180
Arduino Nano v3.0 + soft MultiWii 1.7
Radio Eurgle 9x (ER9X firmware) + receiver
config QuadX
Aloy arm of 50 cm from the center
test propellers 8 and 10 three bladed
ESC calibrated individually and collectively
1) in the GUI MultiWii all is OK I see my gyro and ACC who respond, arming motors, Ok,
as soon as I move throttle up, I have an imbalance in the engine ... Back Left late ( - 180 row) and Front Right also but less
I do the test in Quad+ conf ... ditto 2 unbalanced motors ....
thank you for your responses and feedback ...
PS: flight test ... he take-off bar to the left rear ... logic ...
QuadriX Motors Prob
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- Posts: 1
- Joined: Sat Aug 06, 2011 8:40 am
Re: QuadriX Motors Prob
I have exactly the same problem, anyone got an solution already?